After blowing our first motor at Spokane this summer, we have been working to secure a replacement. After months of dealing with little fiddle parts and taking weeks off, we are finally ready to put “motor 3″ into the car. With this swap, we are also taking the time to finish some things we put off.
The first issue we had was with this freaking pilot bearing. The clutch kit we got included a new one, so I figured, hey lets go it in. In the process of removing the old one, we broke two screw drivers, a slit hammer hook, a special pilot bearing removal tool that was purchased JUST FOR THIS, and at least a couple hours of time. Eventually it was a combination of hack saw blade, broke screw driver, and prying that got it out.

So all I had to do tap the new one in. Exceeeeeeeept I picked a socket that was just slightly too small and broke the bearing.

Good work me. Cut this one too. I managed to find a tech at the local mazda dealer who had one to sell me… but it was 1mm too big. FML
Last sunday we lined the whole crew up and got “motor 2″ (the motor we finished spokane on) out of the car.



We also got a chance to get the new de-powered steering rack in.

With the pilot bearing issue all we could do is wrap the car up and wait til tuesday when the new bearing gets here.

Fast forward to tuesday! The new bearing is in and awesome.

Clutch, on.

The tranny went on pretty easy this time.

Then we found a nice fun new problem! The clutch slave bolts were completely stripped. We had to upside the holes and retap them.


Were going back to the double pulleys. I don’t have a ton of confidence in this solution, but I don’t know what else to do.

Then, wow another problem! Major props to nick for spotting this one. This little wire used to go to what I think was an oil temp sensor. We have never been able to actually get the connector off the sensor so we had to cut it at the track. I got lucky and found the cut sensor in a pile of junk and got it re-attached!


We finished the night off by getting the motor physically back in the car. I had really hoped to get it running by the end of the night but all the little issues we just ran out of time. Still, way better then dealing with it at the track.

The next night after work, we got back on it. Got everything under the car done. Got most of the other stuff hooked up too.


That catches us up to today. The rest of the crew had better things to do (why didn’t I?) and I was left solo finished it off.

I got it far enough to try to start it. Several serious issues:
* Lol i forgot to hook up the throttle cable.
* Clutch needs to be bled. The clutch slave has been on the bench for almost a year. No helpers pretty much made this impossible.
* The gear shift does NOT feel right. I can get it into 2/4 ok but not at all into 1/3/5. Maybe its due to the clutch bleeding and the throwout bearing not being engaged all the way yet?
* Starter spins but doesn’t engage. Welp. We have a third starter, probably time to try it out.
I’m so tired of working on this car. I hope this all works out. Need beer and sleep.