I have been taking some rest time from the race car, I think it has shown in the frequency of updates. I apologize, and promise that it will be picking up again. We have a tentative team ready to go for Spokane at the end of july. Lots of new faces and new energy, it feels good. To help get this next push off, I have a treat! Another engine build
. After our motor failure (due to oiling issues that were my fault, mistakes made during the build) in Portland, we needed yet another rebuild. This time I had several very expensive lessons to leverage.
This time around, I went with all mazda stuff. With the mazda racer sponsorship program it actually ended up being the cheapest too. As usual during the last failure we ruined a bunch of stuff. We got new(to us)/used center iron, front iron, rotors, front counter weight. We also got new side seals, and oil control rings, gaskets, rotor bearings, misc. Were going to reuse our apex seals, corner seals, and everything else not mentioned.

This time around, I spending a lot more time measuring parts and checking tolerances. This is the e-shaft getting checked to make sure its straight.

Cleaning is almost half the work of the whole build. Here is one of the new (to us) rotors cleaned up some.

The irons were pretty rough. Lots of oil and gunk. The coolant seal grooves needed some love too.


More clean up.


Clean up all done, its time to start fitting everything. First off, the side seals come too long from the factory. They have to be individually fit per groove with hand grinding.

… and then disaster. While fitting one of the new rotors, I discovered an issue. It looks like this rotor was dropped. This corner here is bent in. The apex seals and corner seals don’t fit anymore. This rotor is junk now.



So I grabbed one of the rotors from the last build. The front rotor didn’t loose compression and looks ok. It’s within tolerance for weight too. At the end of the clean up day this is where we stood. A couple side seals fit in one rotor and most of the cleaning done.


I continued putting in time after work getting side seals fitted. On the last side of the last rotor (the reused one from our last build), I hit a major problem. The side seals didn’t have enough clearance and were sticking in the grooves. I gave up finding another after a week of searching and said f’it. Time to chump. I have been told by at least two people you can just sand it to get your clearance… (the shop manual says not to do this, lol).

It worked well I think. Its still nice and sharp. I checked the clearance and its spot on now. Side seals done.

I finished marking them up and got the petroleum jelly out to get the final fitment done.

Time to start stacking the motor. I finally broke down and got a pineapple engine stand adapter. It has been well worth the money. Doing work on the engine stand is so nice. Screw the bucket.

Lots more clearance checking.


Were switching out the oil jets on the e-shaft as well. These are race parts that help oil flow. These should help keep things lubed and cooled at high rpms.

New jet on the left, old one with the ball and spring on the right.

Now we are ready to stack. Hylomar is put in the groves. The coolant seals are fit.

The first housing is slid down.

The first rotor is inserted (this time, the right side up
). The e-shaft also makes an appearance here.

Apex seals carefully fit.



The center iron is prepped…

… and then fit to the stack.


While prepping the second rotor I discovered a big issue… I had too many outer coolant seals. That means that I missed one in this stack here. Looking back through the pictures, the mistake was clearly found
. It was missed on the front side of the center iron, so a lot of it had to come apart again. SOP for my builds, sigh.


Rear iron is prep’d.

Second rotor is installed.

With the last iron fit, it was time to get the through bolts in. Too bad they got stored with water in the bag and are now nasty. Time for a second prep/clean up.


Torqued.


Flywheel on.

Front needle bearings fit.

The rest of the front e-shaft parts are fit to test the play.

Within tolerances. On the outer edge, but my other spacer would have made it work. Good enough for chumpcar.


Oil pump fit…

… and the gears and chain.

I need a stop for the flywheel, engine stand makes things easy again.

Front cover oil passage fit properly this time.

The missing oil control plunger was also replaced and installed.


RTV applied and ready to go with the front cover.

Here is that oil passage that was missing the o-ring last time. Looks good this time.

Pulley and bolt installed.

Time for the oil pain. The pickup fitted.


This oil level dealy sensor was leaking before. There will never be a better time to fix it. RTV to the rescue.

RTV ready for the oil pan…

… and fit.

Time to start with the little things. CAS installed as well as the oil dip stick and cap.

EGR block off reinstalled.

5/6th port sleeves reinstalled.
Oil pressure sender installed.

Water pump and it’s housing are cleaned up…

… and installed.


Lower intake manifold (LIM) ready to go on.

Along with it, I also installed the rats nest and wiring harness.

The lower fuel rail and injectors go on.

The UIM (upper intake manifold) goes on and its hooked up.

Throttle body installed.

The last exhaust manifold had an issue last while we took this engine out. One of the studs to the cat back snapped off. These are huge and a giant pain in the butt to drill out. Luckily I have a couple spares. All the spares had some kind of issues though. I picked this one out, since the only issue was this M8 bolt that had snapped its head off. This hardware is used to hold the heat shield on the manifold. I drilled out the hole and retapped it.


Not the best, but it will do. Generous amounts of anti-seize was applied to all hardware touching this manifold this time around.




As the motor sits now. Nearly ready to fit the tranny.


The garage did get a bit blown out.

Ahh that better.

Until thursday old friend!
